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Automatic Lubrication

The ShoeBox compressor now comes standard with an automatic silicone oil system

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Shown here actual size

Shown here actual size, the ShoeBox is the worlds smallest and lightest line of high pressure compressors.

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Two Models

There are two models of ShoeBox Air Compressor. One is set for 4500 psi (300 bar) output, the other is set for 3000 psi (200 bar). ..

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About Us

History behind the ShoeBox Compressor

The ShoeBox Air Compressor was conceived, designed and developed by Tom Kaye. Tom has a twenty year association with the paintball industry and developed many products such as compressed air for paintball markers. Tom retired from paintball in 2005 but decided to come back into manufacturing when he saw tremendous demand for this small home air compressor. More information is available here TomKaye.com

Historic Time Line

04-14-2016 F10 introduced 10 cubic feet per hour.
09-01-2015 New website launched
12-12-2012 Introduced the Freedom8 model 8 cubic feet per hour
4-16-2012 Sold our 1000th compressor!
12-6-2011 Introduced belt drive and hardened pistons.
6-16-2011 Implemented 90 day parts and labor warranty
3-26-2011 We expect to be out of backorder in the next few weeks. 220v motors are now shipping to Europe.
2-2-2011 Compressors are now shipping almost every day.  220v motors for Europe are in testing.
11-25-2010 The second run of 500 units is in assembly. The first 100 should ship out before the middle of December.
8-11-2010 The first run of 100 has sold out and shipped. Overall there were very few problems. Gearing up for the next run of 500 scheduled to start assembly in Sept. I will be back in Chicago again for an extended stay to oversee the production.
3-24-2010 Suppliers are all gearing up for parts production beginning in April. I get a couple weeks off before the fireworks start. I leave for Chicago
4-6-10. My suppliers went from dead to working 3 shifts inside of 6 weeks. Looks like the recession is over but that's going to make it really hard to hold down the cost.
3-17-2010 Finalizing the production blueprints. Purchase orders go out this week hopefully. All the problems I know about are solved, its the ones you don't know....
3-1-2010 New motor solved the overheating problem. The new motor is higher RPM which needs more gear reduction. The chain drive now has two more sprockets. The power switch welded itself. Searching for a better switch.
2-22-2010 Prototype is working well but the motor is overheating. Searching for a new motor.
1-22-2010 Construction of 2 pre-production prototypes begins.
1-12-2010 Finished CAD design of final product.
1-7-2010 First prints go out for quote.
12-18-2009 A two stage piston design is settled on with an 85 psi shop air feed as the best solution.
12-15-2009 A single stage to 4500 is prototyped and tested. It hits 3000 psi but is found to not work well enough for production.
12-12-2009 Poll on Automags.org indicates about half the players could use a 3,000 psi compressor. The other half really want 4500.http://www.automags.org/forums/showthread.php?t=24753312-20-09 New motor that spins at 95 rpm is tested and works well but is expensive.
12-08-09 Prototype compressor fills a tank in under 20 hours with a very slow 16 rpm motor. This was achieved using an 85 psi shop compressor feed.http://www.automags.org/forums/showthread.php?t=24745111-26-09 Players polled on Automags.org about the idea of using a shop air compressor at 85 psi to feed the mini-compressor for faster fill speeds. Most players have a compressor. http://www.automags.org/forums/showthread.php?t=24718511-25-09Prototype hits 4500 psi on first run.
11-2-2009 Three stage piston compressor is machined from scratch. Initial tests are positive but the motor is highly stressed working against three pistons.
10-15-2009 A post to the forum at Automags.org confirms players are very interested in a small compressor http://www.automags.org/forums/showthread.php?t=246171